Sara Kit Certification
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Build Space
Make a copy of:
Main Checklist
Electronics Checklist
Build
Kit Build
Time Lapse
One can study the time lapse in detail to understand the build time. This time lapse should span about 7-8 hours. Rework time was about 1.2 hours.
Time Log
And comments. Time of build is in minutes. Negative sign marks time of rework (not build time).
- 15:42 - Start. Unpack. Weld frame. Set up camera. Includes going from house to workshop. Time: Frame: 37
- 16:19 - Axis assembly start. Y + Z rear. Missing tool: tape spacer. Time: 7
- 16:26 - Error warning: set screw allen wrench short side wore out mid way. Got another one. Time: -2
- 16:28-16:34 - Cleaning out idler pieces . Time: -7
- 16:35 - Tape on bearings. Not needed in practice. Time: 3
- 16:39 - Finished bearing insertion for all axes. Time: 2
- At the beginning, also glued the extruder holder on x carriage so it has time to dry.
- 16:56 - Y left finished - Time: 28 . Technique: belt was inserted during clam-shell build on both axis end-pieces.
- 17:03 - Z back finished - Time: 7
- 17:15 - Y right, Z front done - Time: 12. Total for all axes outside of X - 47
- 17:23 - Y left and Z back axes mounted on frame. Time: 8
- 17:29 - Y right, Z front hung on frame - Time: 6
- 17:32 - Thermistor and PEI fix - Time: -3
- 17:35 - Glue PEI. Time: 13
- 17:48 - One heat bed nut was too small on the inside. Got another. -10
BREAK at 17:58
- 18:53 - Nut catcher holes in idler pieces were droopy, reamed out to fit nuts. -2. Note that this is important only for X axis and bed mount - as the Y and Z don't use the nut catchers.
- 18:55 - Z platform start.
- 18:58 - Z platform done (without bed attachment still) Time: 3
- 19:10 - X axis done. Time: 12.
- 19:15 - Y endstop glued on Y axis. Both endstops inserted into holders and one glued in. Time: 5. Started power supply.
- 19:18 - 5 power supply screws came off. 1 was lost. Power supply power cord zip tie loose and below power supply. Power supply cord fixed to the top. Replaced screws. Time: -4
- 19:22 - Started control panel. MOSFET dangles forward. Need third hole for MOSFET?
- 19:37 - Control panel done. Time: 15. Notes: MOSFET very close to RAMPS. difficult to plug in USB cable.
- 19:39 - Extruder sensor did not fit in extruder sensor holder. Reamed. Time: -1
- 20:10 - Extruder finished - Time: 32
- 20:21 - X axis mounted - Time: 11. Started cable chain. Missing hole for cable chain. Hole drilled. Time: -8. Also, drilled hole in plastic end piece (this neds to be designed into file to avoid drilling)
- 21:18 - Finished cable chain. Moving to belt pegs. Time for cable chain: 49. Cable chain means assembling cable chain pieces, threading all the wires through, and zip tying to cable chain.
- 21:33 - Belt pegs all inserted and all axes tensioned at one time. Pace slowing down late in day. Time: 14. Also, Most belt pegs were too large. Used smaller ones from inventory. Time: -1. Gluing bed to bed nuts.
- 21:50 - Glued bed to platform. Includes mixing and application time for JB Weld Kwik Weld. Moving onto control panel mounting. Time: 17.
BREAK at 21:55
- 22:12 - 1 power wire on back of RAMPS broke off. Second power wire - one wire broke off inside terminal. Resoldered with solid 12 gauge house wire. Did not fit in terminals, so I shaved some off with a knife. time: -18. This is a recurrent problem. Replace power wires with solid 14 gauge house wire, except for MOSFET wires. When bending these wires, hold wires with both hands to bend.
- 22:30 - Mounted control panel. Note: way over time. Fought the difficult hole locations for a bit of time. Edges of plexiglass were broken on 2 sides - this should be 10 minutes or less under normal circumstances, but took 25 minutes. So I call this: time: -15. Time: 10.
- 22:50 - Made all of the wire connections, plugged everything in, while routing wires neatly and zip tying. Time: 25. (includes 5 minutes before break)
- 23:10 - LCD location incorrect. Removed LCD and used spacer to free up interference from cable chain. Time: -12. Note: could have redrilled location in plexiglass, but didn't want to risk breaking plexiglass late in the night.
- 23:22 - Spool holder holes too small. Reamed first with drill, did not work, so used heat gun to soften plastic, then they went on correctly. Time: -14. Time to actually put on rod holders: 2
- 23:38 - Motion testing. One stepper cable was broken. Replaced with new one after testing broken one on a working motor. Time including replacing one broken wire: 22.
- 0:00 - Printing sample cube. Successful first print with first guess of -1.4 z offset. Didn't have to touch babystepping. Probe triggered correctly without requiring initial probe height readjustment. Time: 5.
- 0:05 - Ran a test print of motor piece. Beginning of production tuning.
Total Time
- 316 minute total build time - not counting any rework steps. Note 1 hour for build of 5 axes from kit.
- Rework total time: 97
- Total break time: 72
TOTAL - 485 minutes, or 8.1 hours
Tips and Tricks
- To level print bed for mounting - press down all the way until the bed mounting idlers both rest on the frame - thereby using the frame to determine a perfect parallel to the ground.
Issues Log
- 2 top half circles of carriage pieces all had extra plastic on them. Needed cleaning.
- Thermistor head was on top face, not in hole:
Evaluation
Overall kit evaluation is this based on Kit Certification#Evaluation
Sara Comments and Improvements
Links
- Kit Certification
- Current Material inventory - [1]
- 3D Printer Logs - for parts production